Structural
Mistuning Analysis
N&R has been investigating the impact of structural
mistuning of centrifugal compressors on high cycle
fatigue life. ANSYS has been used to determine
the tuned structural response and the Turbo-REDUCE
code to determine the additional stresses due
to mistuning. Results show an approximately 30
percent increase in response amplitude because
of frequency mistuning of the impeller. The probabilistic
impact of key geometrical uncertainties such as
blade backsweep angle has also determined.
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Impeller modal
analysis performed for mistuning analysis.
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